My intent was another one and done with a small raise in the launch rpm to hopefully leave on more boost, no such luck. It left ok with a 1.39 60 foot, but just was not making any power and only ran a 10.16. checked the data log, low boost. I took apart the manual boost controller and found a piece of trash, cleaned it out and went back to the lanes. The second pass and she left way better and was on a pass until @1100 feet and I felt it lay over, crap! I quickly scanned the rear mirror, DEATH SMOKE!! All I could think of and kept repeating in my head was please don't oil the tires, please don't oil the tires. I safely made it to the turnoff and it was hardly running so I turned it off. I got a tow back to the pits and promptly pulled the plugs starting on the drivers side as they are easier to get to. #1 looked ok, just wet, #3 had a bent electrode, #7 was fine but a little wet as well. #5, well it wouldn't come out at first, PROBLEM! Seems something large hit #5 and it was now oval shaped, not positive. I stuck a camera in #5 and it looked pretty bad, spun the motor over and the piston didn't move. Needless to say, the end of dragweek 2016 due to a broken rod. Best guess is it pulled apart, I have yet to pull the head and do any other investigation and have already started on a new power plant. Another 5.3, just with a forged rotating assembly, pistons should be here tomorrow. I have gone back and checked the data log on that pass and everything looks good up to that point in the run, so I guess that rod just reached the end of it's life. The time slip was a 1.36 60 foot, 5.7x@120 to 1/8th and 9.06@147 at the stripe, should of been a nice high 8 second pass.
I will download some pics of the plug when I get a chance and some of the internal carnage once I pull it apart. I also have a video from inside on the first day I will try and upload. In the other lane was none other than Larry Dixion the Top fuel Driver. Kind of nice to be able to say that I beat him, but then again, he finished the week and I didn't.
